Ok then a update to where the mk1 is at !!
I got it all good to go to IMM but no real shake down was carried out so I stuck it on a trailer, as I would run it in down there.
So anyway we got to the IMM and all was good. I used the time to sort a problem I had with the dip beam and John said "let's go for a little drive". It all started off good and the mk1 was running sweet. Just to point out I had set it to 5psi and that's where I was planning to keep it, when we got on the dual carriageway John said "******* me this is quick" at that point I turned the BIG RED fun button
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and went to 22psi all was good and the mk1 felt the best it ever has!!! I did have some vids but some one lost his phone :-/
Next day came and we got up and went for a TM road race (who could get To Asda first!) I had Shauna with her GoPro as my co pilot, I am sure some vids might pop up in time.
When we set off back to camp the mk1 was well down on power! I was thinking **** I have seen this before! so we got back and did a TM 1hr head gasket check but all was good hmmmmm then as I bent down pick out a fag I had dropped I saw that the down pipe was hanging off. So I popped it on and I was back in the fight
So I said to Steve come on we will have a test drive on the back road. All was good and it was back to the way it should be and then nothing!!! No drive just lots of revs I had all gears but I could not move :-(
So the TM pit crew was deployed and we cracked open the beers to work out what has gone wrong. We first came up with that it could be the clutch plate let go, so I need a new puller why not have a look here, so Mike and I go and seal the deal on a plate and a puller, as John gets pissed.
All was fine when we pulled it, so I was thinking the pinion nut could of came off, as it had before so we stuck it on the trailer and got on it!
Fast forward a day..
So i pull the engine, and set a new PB should I point out lol, strip it all down but all was good,, very confused so I sat back and had a drink and a fag, then I was thinking maybe the alloy flange had let go, so I give the drive shafts a good wiggle and they were fine. Then I started to look at the balls in the pot joints all was good till one fell off in my hand!!! **** the bed! I had snapped the end of my shaft off!! And it was stuck in the pot joint.
So I stuck the engine back together but as I was doing it upside down I must of mis-aligned it, at first as the mean bolt had hit the windage tray and bent it . As I did not find out until I was doing the flywheel up and I could hear it rubbing so all came apart again :-/
I was pissing about with it with no luck I ripped it out, and moved on with the rebuild, drop it all back in and flushed it with some cheap oil and fired it up
As of tonight it's good to go for a good session on the RR as a good shakedown and to see what it's making
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Husband and wife bonding
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Back in and new oil in
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Fingers crossed I will be running this weekend
Well today went well!
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And made this...
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It was wheel spinning like mad, even with two of us in it and two sat on the wings lol.
But it made 195bhp and 211 ft lbs of torque
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on a cool day that's well over the 200
Thanks for looking simon