For this Part 1 I will address the fuel and ignition system I am planning on using.
When I got this car it had been setting for almost 3 yrs.
The engine steady and clutch end motor mount were broken which allowed the motor to beat the waxstat carb into the firewall. (note the rope tieng the engine steady!!!)
The transmission or transfercase gears sounded like C**p and it had bad vibrations. The more i fixed the more I found wrong.
This is what I started with..it actually cleaned up pretty good!! Typical small bubbles of rust starting in spots.




Well I did some research and found out the motor had already been swapped from a 998 to a 1098.
Since this is my first "mini" I was not sure how much of the noise was normal!!
So I started cleaning things up and getting everything working.
replaced all the motor mounts, pulled the carb and rebuilt it. Put all back together and fired it up. First drive was neat but the ride left a lot to be desired. So I started searching for places to get parts that the VAT and GB post cost would not double the price of!!!!
Minimania in the US carries a lot but if I have to pay those prices I won't be driving the mini much!! Did I mention I live in Italy right now?
But I did find Dave at www.GBcarsparts.com I think he carries a lot of minisports stuff and seems to be the cheapest. And he doesn't gouge shipping to FPO's(can only use USPS.)
I also met another Yank (starrider) living in London here on the board and he has really helped forwarding parts to me.
So that was my introduction to mini's. I got it running enough to drive...then I started to upgrade it.
First was the suspension. In went Hi-lo's and some new cones, monroe shocks, ball joints , tie rod ends, rebuilt the rack and pinion, rebuilt the alternator, bla...bla...bla...
The motor seemed to a little weak and like I said, she had some noises.
Well I picked up a 940 head and decided to give it a try.
Pocketed the block, installed the head, modified the 1098 rockers to work.
Fired it up and was fairly impressed with the new power.
Changed the oil and decided to install the magnetic drain plug. oops
Can't get it all the way in. Pull it back out and metal is stuck all over it......hmm
So I clean it all out and continue on.
Motor runs real good for about 1 week, then it starts smoking more and more.
Guess the rings didn't like the new compression ratio!!
Besides the noise in the tranny and vibration getting worse, I figured it was time to bite the bullet.
I had picked up a 97 MPI short block and tranny for free. Well you know how free goes...
So I decided this is my new powertrain for the mini....
Did I mention this was my first mini?????
Well I really started to learn how much they changed over the years!!
I will do a seperate Part 2 for the motor and head assembly!!
Edited by Bill USN-1, 02 January 2007 - 10:57 PM.