Forgot to update the thread for a couple months in my rush to get moving on this.
Thought I'd take the bitumen up off the floor while the interior was empty, pretty horrible job with the heatgun and scraper and then white spirit on a rag but it came up okay:
Cleaned it up with a wire brush where needed, spot primed where I'd gone to metal and then gave it a brush coat of 2k:
Pretty happy with how it came out to say it's going to be covered by carpet. I forgot to take pictures of this, but the front windscreen came out so I could swap the top dash rail over for one in slightly better nick. Cracked the old screen getting it out so I was pretty nervous about the new one going in, fortunately it went in without too much drama.
The original loom had been bodged a bit and I happened to find a nice tidied up cloth wrapped loom on Facebook for cheap, it'd been fitted to a car since it was done and a couple connectors had been damaged during removal so I repaired that and fitted it. Looks pretty neat with the stainless p-clips holding it along the inner wing:
Front lights refitted with stainless rings and the older style indicators with the metal retaining rings. Using LEDs for everything but the indicators.
Stripped down the wiper mechanism, cleaned and re-greased it, fitted with new black arms. They still sag a bit towards the bottom of the screen and are generally a bit crap, so possibly more work to do there.
I originally had 1/2 hoses running from the lower rad hose and inlet manifold through the bulkhead and some 1/2" to 5/8" joiners inside the cabin. It kept kinking the hoses and generally looking a bit rubbish. So here's my solution:
These bulkhead fittings secure to the bulkhead plate and give me a nice 90 degree angle inside to run the heater hoses:
The heater box could use a clean up and the fan is a bit noisy, but that's a job for over winter. I really wanted to get it through it's MOT before the weather turned...
Took it in for it's test a couple weeks ago and though I had a couple dramas getting there I had to keep pulling over and tweaking the carb, but happily it passed with flying colours!
I've only driven it for about 30 minutes, but I've got a list of niggles to sort:
- Next morning after parking it up I noticed a dribble of coolant from the top hose. I'd had problems getting the rad end of the bottom hose not to leak resulting in a rad remove/refit 30 mins before the MOT. I've looked at this since and the bottom hose is seemingly murder for not sealing if it's even slightly off being squarely fitted. I ended up fitting the bottom hose off the car with the open ends all blocked up and pressure testing it and adjusting the position until it sealed ok. It's a brand new rad, hose and genuine stainless jubilee clip so I've no idea why this has proved such a faff. When I refitted it the water pump end leaked - the breather canister puts pressure on it and pushes it off square. Removed the breather to refit the hose square and tighten it before refitting the canister (but that involved taking the inlet manifold off, took a whole day to sort this all told...).
- The idle is too high, like 1200rpm and sticks. I've looked since and think the throttle cable was a bit too tight so I've adjusted that, yet to pull it out and try it again.
- I messed up with the speedo. I thought I had the post 84 smiths 90mph clocks and so fitted 6/16 speedo drives. It ended up underreading by about 10%. Turns out I have the "Smiths early tri clock" and the gears already fitted were the correct ones... the gear behind the engine mount is a pain to get to so I really wasn't happy about doing this again. I've got this refitted but now struggling to get the speedo cable to click into the clocks again...
- There's a rattle/rubbing noise driving me insane, sounds like it's coming from the back of the car. I thought it might be the plastic trim fitted around the roof line so I've removed that, but also might be the rear seat back rubbing against the parcel shelf. Need to road test again to figure this out.
- Driver side front wheel is rubbing the arch, even raised up an extra inch and the tie bar lengthened. Hoping this gets a little better when I switch to 10s and gain a bit of clearance, but not sure if changes in offset will, um, offset that.