Overdue update.
The new 1330cc engine is in. It is sitting on the original but refurbished gearbox which now has an x-pin diff. I cleaned up and put back the old cylinder head. Happy with the valve size!
Got the Weber refurbished as well and fitted to a longer manifold.
Fitted HiLos and new red spot cones to the front suspension.
As the new engine is A+ I couldn't refit the old distributor. So I went for the SC ignition management system with a TPS on the Weber. Thinking being that this would be a good future proofing for engine changes going forward.
Everything was back together and rolling road tuned for the MK1 Action Day at Blyton Park where I met a new friend!
and my co-driver tried out his smart new video camera before disappearing to South Africa to film his pop star client!
https://youtu.be/nRtPMPWsnNU