998 70k, 65d electronic dizzy timed to 8 degrees, vac advance disconnected as had been for the last 6 years with no problems.
Last month the mini started misfiring, almost as if the ignition was temporarily being switched off with the alternator light coming on below 2000 rpm. Worse with the choke out needed to keep it above 2k and close to undriveable. As it also cuts out when the clutch is depressed when coming to a stop with the choke in/engine warm. Where the engine goes completely silent (so no warning) and the alternator light comes on and restarts instantly on the key.
Started on morning of mot. Witch after a hill start with lots of choke to keep it above 2k and stop it from stalling/ misfiring causing lots of blue smoke (probably bore wash) it cleared once warm. Passed mot with 2.3% CO and 317 ppm HC, but has been undriveable since.
Have so far done the plugs, leads looked ok, new dizzy carp and rotor, new ignition module, borrowed working coil from other mini, and checked the wiring and connectors. Reconnected vac advance witch had been disconnected for last 6 years, thought it was “fixed” until the carb was dumping fuel out of the overflow.
So have also stripped and cleaned the carb, renewed the gaskets, relapped and adjusted the needle valve, replaced the fuel pump to carb line doing away with inline filter. Fixed the sticking choke after the carb was refitted, stripped dizzy, sprayed innards and refitted. Only for it to still be doing it as before.
Recap, it idles all day fine, revved between idle and 2k misfiring/cutting out (but still running) alternator light on, above 2k all as normal right up to 5.5k.
Edited by 1984mini25, 10 October 2015 - 10:31 PM.