Thought I should update this!
Well it survived its week use, but barely!
So replacing the filter head completely sorted the oil leak and then she ran ok for a day.
The running then got gradually worse, it got really bad. I feared it wouldn't get me to work, and really had no confidence in it making the 130 miles back home!
I tried adjusting the fueling and timing, and checking everything but couldn't get it to run right.
I managed to chug it home last Friday and on a 190 mile detour! 300 miles in one go!
With the problems it was having that was incredibly stupid, but I wasn't let down.
But the old girl wasn't happy, had to remove the vac advance just to make it run. It wouldn't pull, and chugged under 2k rpm, it just sounded awful.
I've since rebuilt the distributor and reset the timing (ruined it by filling it with oil from the leaking filter head, and then ruined the timing when replacing the head!
I was hoping to find broken flyweights in the distributor, but alas no, just oil.
So the ignition side is now again spot on.
Sadly this hasnt sorted a horrible chugging at low revs, as soon as you get though this, around 2k rpm it'll pull like a train. Next step is to pull and rebuild the carb!
I hate to say it but climbing back into my freshly serviced daily driver was heaven.
Also doesn't help the minis case that I collected a mod I'd always wanted to do for it that weekend.
I still haven't ruled out Stanford Hall though...
Joe
Edited by 72clubman, 03 September 2015 - 06:47 PM.